- Source: Gimli Glider
Air Canada Flight 143, commonly known as the Gimli Glider, was a Canadian scheduled domestic passenger flight between Montreal and Edmonton that ran out of fuel on Saturday, July 23, 1983, at an altitude of 41,000 feet (12,500 m), midway through the flight. The flight crew successfully glided the Boeing 767 to an emergency landing at a former Royal Canadian Air Force base in Gimli, Manitoba, which had been converted to a racetrack, Gimli Motorsports Park. It resulted in no serious injuries to passengers or persons on the ground, and only minor damage to the aircraft. The aircraft was repaired and remained in service until its retirement in 2008. This unusual aviation accident earned the aircraft the nickname "Gimli Glider."
The accident was caused by a series of issues, starting with a failed fuel-quantity indicator sensor (FQIS). These had high failure rates in the 767, and the only available replacement was also nonfunctional. The problem was logged, but later, the maintenance crew misunderstood the problem and turned off the backup FQIS. This required the fuel to be manually measured using a dripstick. The navigational computer required the fuel to be entered in kilograms; however, an incorrect conversion from volume to mass was applied, which led the pilots and ground crew to agree that it was carrying enough fuel for the remaining trip. The aircraft was carrying only 45% of its required fuel load. The aircraft ran out of fuel halfway to Edmonton, where maintenance staff were waiting to install a working FQIS that they had borrowed from another airline.
The Board of Inquiry found fault with Air Canada procedures, training, and manuals. It recommended the adoption of fuelling procedures and other safety measures that U.S. and European airlines were already using. The board also recommended the immediate conversion of all Air Canada aircraft from imperial units to metric units, since a mixed fleet was more dangerous than an all-imperial or an all-metric fleet.
Aircraft
The aircraft involved, manufactured in 1983, was a Boeing 767-233 registered as C-GAUN with serial number 22520. It was powered by two Pratt & Whitney JT9D-7R4D engines.
History
= Background
=On July 22, 1983, Air Canada Boeing 767 C-GAUN underwent routine checks in Edmonton. The technician found a defective FQIS, so he disabled the defective channel, and made an entry in the logbook. The next morning, Captain John Weir and co-pilot Captain Donald Johnson were told about the problem. Since the FQIS was now operating on a single channel, a dripstick reading was taken to obtain a second fuel quantity measurement. Weir converted the dripstick reading from centimetres to litres to kilograms, finding that it agreed with the FQIS. The plane flew to Toronto and then Montreal without accident.
At Montreal, Captain Robert "Bob" Pearson and First Officer Maurice Quintal took over the airplane for Flight 143 to Ottawa and Edmonton. During the handover, Weir told Pearson that a problem existed with the FQIS, and Pearson decided to take on enough fuel to fly to Edmonton without refuelling in Ottawa. Meanwhile, an avionics technician had entered the cockpit and read the logbook. While waiting for the fuel truck, he enabled the defective channel, and performed an FQIS self-test. Distracted by the arrival of the fuel truck, he left the channel enabled after the FQIS failed the test. Pearson entered the cockpit to find the FQIS blank, as he expected.
After taking a dripstick measurement, Pearson converted the reading from centimetres to litres to kilograms. However, he did his calculation with the density figure for jet fuel in pounds/litre from the Air Canada refueler's slip, used for all other aircraft in the fleet, instead of kilograms/litre for the all-metric 767 aircraft, which was new to the fleet. Since the FQIS was not operational, he entered the reading into the flight management computer, which tracked the amount of fuel remaining in kilograms. The airplane flew to Ottawa without accident, where another dripstick measurement was taken and converted using the density in pounds/litre. Since the aircraft appeared to have enough fuel to reach Edmonton, no fuel was loaded at Ottawa.
= Running out of fuel
=While Flight 143 was cruising over Red Lake, Ontario at 41,000 feet (12,500 m) shortly after 8 pm CDT, the aircraft's cockpit warning system sounded, indicating a fuel-pressure problem on the aircraft's left side. Assuming that a fuel pump had failed, the pilots turned off the alarm, knowing that the engine could be gravity-fed in level flight. A few seconds later, the fuel pressure alarm also sounded for the right engine. This prompted the pilots to divert to Winnipeg.
The left engine failed within seconds, and the pilots began preparing for a single-engine landing. As they communicated their intentions to controllers in Winnipeg and tried to restart the left engine, the cockpit warning system sounded again with the "all engines out" sound, a sharp "bong" that no one in the cockpit could recall having heard before. The right-side engine stopped seconds later, and the 767 lost all power. Flying with all engines out was never expected to occur, so it had never been covered in training. Adding to both the crew's and the controllers' problems, the plane's transponder failed, stopping the altitude reporting function, and forcing the controllers to revert to primary radar to track the plane.
The 767 was one of the first airliners to include an electronic flight instrument system, which operated on the electricity generated by the aircraft's jet engines. With both engines stopped, the system went dead, and most screens went blank, leaving only a few basic battery-powered emergency flight instruments. While these provided sufficient information to land the aircraft, the backup instruments did not include a vertical speed indicator that could be used to determine how far the aircraft could glide.
On the Boeing 767, the control surfaces are so large that the pilots cannot move them with muscle power alone. Instead, hydraulic systems are used to multiply the forces applied by the pilots. Since the engines supply power for the hydraulic systems, in the case of a complete power outage, the aircraft was designed with a ram air turbine that swings out from a compartment located beneath the bottom of the 767, and drives a hydraulic pump to supply power to hydraulic systems.
= Landing at Gimli
=In line with their planned diversion to Winnipeg, the pilots had been descending through 35,000 feet (10,700 m) when the second engine shut down. They had searched their emergency checklist for the section on flying the aircraft with both engines out, only to find that no such section existed. Captain Pearson was an experienced glider pilot, so he was familiar with flying techniques rarely used in commercial flight. Pearson needed to fly the 767 at the optimum glide speed to have the maximum range and, therefore, the largest choice of possible landing sites. Making his best guess as to this speed for the 767, he flew the aircraft at 220 knots (410 km/h; 250 mph). First Officer Quintal began to calculate whether they could reach Winnipeg. Quintal used the altitude from one of the mechanical backup instruments, while the distance travelled was supplied by the air traffic controllers in Winnipeg, measured by the aircraft's radar echo observed at Winnipeg. In 10 nautical miles (19 km; 12 mi), the aircraft lost 5,000 feet (1,500 m), giving a glide ratio of roughly 12:1 (dedicated glider planes reach ratios of 50:1 to 70:1).
At this point, Quintal proposed landing at the former RCAF Station Gimli, a closed air force base where he had once served as a pilot for the Royal Canadian Air Force. Unbeknownst to Quintal or the air traffic controller, a part of the facility had been converted to a race track complex, now known as Gimli Motorsports Park. It included a road-race course, a go-kart track, and a dragstrip. A Canadian Automobile Sport Clubs-sanctioned sports-car race hosted by the Winnipeg Sports Car Club was underway at the time of the accident. The area around the decommissioned runway was full of cars and campers. Part of the decommissioned runway was being used to stage the race.
As the aircraft slowed on approach to landing, the reduced power generated by the ram air turbine rendered the aircraft increasingly difficult to control. Without main power, the pilots used a gravity drop to lower the landing gear and lock it into place. The main gear locked into position, but the nose wheel did not. The failure of the nose wheel to lock would later prove to be a serendipitous advantage after touchdown for the safety of those on the converted runway.
As the plane approached the runway, the pilots realized it was coming in too high and fast, increasing the likelihood that the 767 would run off the runway. The lack of hydraulic pressure prevented flap/slat extension that would have, under normal conditions, reduced the aircraft's stall speed and increased the lift coefficient of the wings, to slow the airliner for a safe landing. The pilots briefly considered a 360° turn to reduce speed and altitude, but they decided they did not have enough altitude for the manoeuvre. Pearson decided to execute a forward slip to increase drag and reduce altitude. This manoeuvre, performed by "crossing the controls" (applying the rudder in one direction and ailerons in the other direction), is commonly used in gliders and light aircraft to descend more quickly without increasing forward speed; it is rarely used in large jet airliners outside of rare circumstances like those of this flight. The forward slip disrupted airflow past the ram air turbine, which decreased the hydraulic power available; the pilots were surprised to find the aircraft slow to respond when straightening after the forward slip.
With both engines completely starved of fuel, the plane made hardly any noise during its approach. This gave people on the ground no warning of the impromptu landing and little time to flee. As the gliding plane closed in on the decommissioned runway, the pilots noticed boys were riding bicycles within 1,000 feet (300 m) of the projected point of impact.
Two factors helped avert disaster: the failure of the front landing gear to lock into position during the gravity drop, and a guardrail installed along the centre of the repurposed runway to facilitate its use as a drag race track. Pearson braked hard as soon as the wheels touched down on the runway, skidding and promptly blowing out two of the aircraft's tires. The unlocked nose wheel collapsed and was forced back into its well, causing the aircraft's nose to slam into, bounce off, and then scrape along the ground. This additional friction helped to slow the airplane, and kept it from crashing into the crowds surrounding the runway. Pearson applied extra right brake, which caused the main landing gear to straddle the guardrail. Air Canada Flight 143 came to a final stop on the ground 17 minutes after running out of fuel.
No serious injuries occurred among the 61 passengers or the people on the ground. As the aircraft's nose had collapsed onto the ground, its tail was elevated, so some minor injuries occurred when passengers exited the aircraft via the rear slides, which were not sufficiently long to accommodate the increased height. Racers and course workers with portable fire extinguishers extinguished a minor fire in the nose area.
Investigation
The Aviation Safety Board of Canada (predecessor of the modern Transportation Safety Board of Canada) reported that Air Canada management was responsible for "corporate and equipment deficiencies." Their report praised the flight and cabin crews for their "professionalism and skill." It noted that Air Canada "neglected to assign clearly and specifically the responsibility for calculating the fuel load in an abnormal situation.": 65 It further found that the airline had failed to reallocate the task of checking fuel load (which had been the responsibility of the flight engineer on older aircraft flown with a crew of three). The safety board also said that Air Canada needed to keep more spare parts, including replacements for the defective fuel quantity indicator, in its maintenance inventory, and provide better, more thorough training on the metric system to its pilots and fuelling personnel. The final report of the investigation was published in April 1985.
= Fuel-quantity indication system
=The amount of fuel in the tanks of a Boeing 767 is computed by the FQIS and displayed in the cockpit. The FQIS on the aircraft was a dual-processor channel, each independently calculating the fuel load and cross-checking with the other. In the event of one failing, the other could still operate alone, but in that case, the indicated quantity was required to be cross-checked against a floatstick measurement before departure. If both channels fail, no fuel display was seen in the cockpit, and the aircraft would be considered unserviceable and not authorized to fly.
Because inconsistencies had been found with the FQIS in other 767s, Boeing issued a service bulletin for the routine checking of this system. An engineer in Edmonton duly did so when the aircraft arrived from Toronto following a trouble-free flight the day before the accident. While conducting this check, the FQIS failed, and the cockpit fuel gauges went blank. The engineer had encountered the same problem earlier in the month when this same aircraft had arrived from Toronto with an FQIS fault. He found then that disabling the second channel by pulling the circuit breaker in the cockpit restored the fuel gauges to working order, albeit with only the single FQIS channel operative. Without any spares, he repeated this temporary fix by pulling and tagging the circuit breaker.
A record of all actions and findings was made in the maintenance log, including the entry: "SERVICE CHK – FOUND FUEL QTY IND BLANK – FUEL QTY #2 C/B PULLED & TAGGED...". This reports that the fuel gauges were blank and that the second FQIS channel was disabled, but it does not make clear that the latter fixed the former.
The aircraft flew from Edmonton to Montreal on the day of the accident. Before departure, the engineer informed the pilot of the problem and confirmed that the tanks must be verified with a floatstick. In a misunderstanding, the pilot believed the aircraft had been flown with the fault from Toronto the previous afternoon. The flight to Montreal proceeded uneventfully, with fuel gauges operating correctly on the single channel.
On arrival in Montreal, a new crew boarded for the return flight to Edmonton. The outgoing pilot informed Captain Pearson and First Officer Quintal of the problem with the FQIS and passed along his mistaken belief that the aircraft had flown the previous day with this problem. In a further misunderstanding, Captain Pearson believed he was also being told that the FQIS had been completely unserviceable since then.
While the aircraft was being prepared to return to Edmonton, a maintenance worker decided to investigate the problem with the faulty FQIS. To test the system, he re-enabled the second channel, at which point the fuel gauges in the cockpit went blank. However, before he could disable the second channel again, he was called away to perform a floatstick measurement of fuel remaining in the tanks, leaving the circuit breaker tagged (which masked the fact that it was no longer pulled). The FQIS was now completely unserviceable, and the fuel gauges were blank.
On entering the cockpit, Captain Pearson saw what he was expecting to see—blank fuel gauges and a tagged circuit breaker. Pearson consulted the master minimum equipment list (MMEL), which indicated that the aircraft was not legal to fly with blank fuel gauges. Still, due to a misunderstanding, Pearson believed it was safe to fly if the amount of fuel was confirmed with measuring sticks.
The 767 was still a very new aircraft, having flown its maiden flight in September 1981. C-GAUN was the 47th Boeing 767 off the production line and had been delivered to Air Canada fewer than four months prior to this flight. In that time, 55 changes had been made to the MMEL, and some pages were blank pending development of procedures.
Because of this unreliability, maintenance personnel authorizing flights had become standard practice. To add to his misconceptions about the aircraft's flying condition since the previous day, reinforced by what he saw in the cockpit, Pearson now had a signed-off maintenance log, which had become customarily preferred over the MMEL.
= Miscalculation during fuelling
=In older aircraft with a three-person crew, the flight engineer kept a fuel log and supervised the fuelling. The Boeing 767 belonged to a new generation of aircraft that flew with only a pilot and co-pilot, but Air Canada had not clearly assigned responsibility for supervising the fuelling.: 64–65 On the day of the accident, two technicians and two pilots worked on the calculation in Montreal. One technician stopped after he found that he was not making any progress. Another technician was using a piece of paper in his pocket, and he stopped when he ran out of space. First Officer Quintal did the calculation by hand, and Captain Pearson checked the arithmetic with his Jeppesen slide rule.: 40–41
Since the FQIS was not working, Captain Pearson decided to take on enough fuel to reach Edmonton without refuelling at Ottawa.: 26 The flight plan showed that 22,300 kilograms (49,200 lb) of fuel were required for the flight from Montreal to Ottawa to Edmonton. A dripstick check found that 7,682 litres (1,690 imp gal; 2,029 US gal) of fuel was already in the tanks. To calculate how much fuel the airplane had to take on, he needed to convert the 7,682 litres of fuel already in the tanks to their equivalent mass in kilograms, subtract that figure from the 22,300 kg total fuel that would be needed, and convert that result back into its equivalent volume.: 41 The density in metric units was 0.803 kg/L, so the correct calculation would have been:
7,682 L × 0.803 kg/L = 6,169 kg = mass of fuel already on board
22,300 kg − 6,169 kg = 16,131 kg = mass of additional fuel required, or
16,131 kg ÷ (0.803 kg/L) = 20,088 L = volume of additional fuel required
At the time of the accident, Canada's aviation sector was converting from imperial to metric units. As part of this process, the new 767s acquired by Air Canada were the first to be calibrated for metric units.: 63–64 The fueler reported that the density of jet fuel at the time was 1.77, which was in lb/L, since other Air Canada aircraft used lb. Pearson and Quintal both used the density of jet fuel in lb/L without converting to kg/L:: 40–41
7,682 L × 1.77 lb/L = 13,597 lb = misinterpreted as kilograms of fuel already on board
22,300 kg − 13,597 kg = 8,703 kg = incorrect mass of additional fuel required
8,703 kg ÷ (1.77 lb/L) = 4,917 L·kg/lb = misinterpreted as litres of additional fuel required
Instead of taking on the 20,088 litres (4,419 imp gal; 5,307 US gal) of additional fuel that they required, they took on only 4,917 litres (1,082 imp gal; 1,299 US gal). The use of the incorrect conversion factor led to a total fuel load of only 22,300 lb (10,100 kg) rather than the 49,170 lb (22,300 kg) that were needed. This was less than half of the amount required to reach their destination.
The flight management computer (FMC) measures fuel consumption, allowing the crew to keep track of fuel burned as the flight progresses. It is normally updated automatically by the FQIS, but the fuel quantity can also be entered manually. Because the FMC would reset during the stopover in Ottawa, the captain had the fuel tanks measured again with the dripstick. With 11,430 litres (2,510 imp gal; 3,020 US gal) of fuel in the tanks, the fueler gave a density of 1.78. Repeating the same error, Captain Pearson determined that he had 20,400 kg (45,000 lb) of fuel and entered this number into the FMC. However, he actually had just 9,250 kg (20,400 lb) of fuel.: 42–43
The previous flight from Edmonton to Montreal had avoided the error. The fueler at Edmonton knew the density of jet fuel in kg/L, and he calculated the correct number of litres to pump into the tanks. He testified that it was a "regular practice of his" to do such calculations. When fuelling was complete, Captains Weir and Johnson checked the figures. The captain knew "from previous experience" the density of jet fuel in kg/L. He also had a working FQIS, which agreed with his calculations.: 43–44
Aftermath
Following Air Canada's internal investigation, Captain Pearson was demoted for six months, and First Officer Quintal was suspended for two weeks for allowing the accident to happen. Three maintenance workers were also suspended. In 1985, Pearson and Quintal were awarded the first ever Fédération Aéronautique Internationale Diploma for Outstanding Airmanship. Several attempts by other crews who were given the same circumstances in a simulator at Vancouver resulted in crashes. Quintal was promoted to captain in 1989. Pearson remained with Air Canada for ten years and then moved to flying for Asiana Airlines; he retired in 1995. Maurice Quintal died at the age of 68 on September 24, 2015, in Saint-Donat, Quebec.
The aircraft was temporarily repaired at Gimli and flew out two days later to be fully repaired at a maintenance base in Winnipeg. The aircraft was returned to service with Air Canada after the full repair. Following a successful appeal against their suspensions, Pearson and Quintal were assigned as crew members aboard another Air Canada flight.
The 1995 television movie Falling from the Sky: Flight 174 is loosely based on this event.
The Discovery Channel Canada / National Geographic TV series Mayday covered the accident in a 2008 episode titled "Gimli Glider". The episode featured interviews with survivors, including Pearson and Quintal, and a dramatic flight recreation.
Retirement
After almost 25 years of service, C-GAUN flew its last revenue flight on January 1, 2008. The Gimli Glider then began its final voyage on January 24, 2008, as AC7067, from Montreal Trudeau to Tucson International Airport and final flight to retirement at California's Mojave Airport. The flight was captained by Jean-Marc Bélanger, a former head of the Air Canada Pilots Association; captains Robert Pearson and Maurice Quintal were also on board, as were three of the six flight attendants from Flight 143.
That summer, on July 23, 2008, the 25th anniversary of the accident, pilots Pearson and Quintal were celebrated in a parade in Gimli, and a mural was dedicated to commemorate the landing.
In April 2013, the Gimli Glider was offered for sale at auction, by a company called Collectable Cars, with an estimated price of CA$2.75–3 million. However, bidding only reached CA$425,000 and the lot was unsold.
According to a website dedicated to saving the aircraft, the Gimli Glider was scrapped in early 2014. Parts of the metal fuselage skin were made into 10,000 sequentially numbered luggage tags, and as of 2015, were offered for sale by a California company, MotoArt, under the product name "PLANETAGS".
In June 2017, a permanent museum exhibit of the event opened in Gimli. The exhibit includes a cockpit mock-up flight simulator, and as of July 2017, sold event memorabilia.
See also
List of airline flights that required gliding
List of accidents and incidents involving commercial aircraft
Cornfield Bomber
References
Further reading
External links
The Official Gimli Glider Project website
Damn Interesting: The Gimli Glider
CBC Digital Archives: 'Gimli Glider' lands without fuel
Photo of C-GAUN after the landing
Picture of C-GAUN in storage (airliners.net)
Video of retirement fly-by on YouTube
Kata Kunci Pencarian:
- Air Canada Penerbangan 143
- Glider
- Avianca Penerbangan 052
- Bandar Udara Internasional Montréal–Pierre Elliott Trudeau
- Daftar kecelakaan dan insiden pesawat penumpang
- Gimli Glider
- Gimli
- RCAF Station Gimli
- Gimli, Manitoba
- Glider
- Boeing 767
- Gimli Industrial Park Airport
- Rural Municipality of Gimli
- Falling from the Sky: Flight 174
- Air Transat Flight 236